Threesixes
Viper Owner
- Joined
- Feb 2, 2010
- Posts
- 55
- Reaction score
- 0
Hey all,
My car (05 srt-10, stock)had a tiny power steering leak from where the top hose went into the pump. It would leave a real small puddle underneath the car every day but never made the fluid level low or anything.
Well today I took the hose off and the o-ring looked ok so I just put it back on and figured Id order a new hose. After I put it back together I tried to bleed it by jacking it up and going lock to lock many times, then let it run for awhile.
It worked great for about three or four minutes then I lost power steering and fan and the car got very hot. Almost pegged the gauge. I kept repeating the bleeding procedure and nothing. So I took it back apart and put it back together and the same thing. Worked great for a few minutes then nothing. Im so frustrated, I think theres air trapped somewhere. Anyone else have this issue?
Also when I pulled the hose off, the fitting underneath the hose that goes into the pump came off. There was a bigger o-ring on that but it looked ok too. Underneath that there was a little black springy plunger thing. Not sure if disturbing that may have something to do with it?
Any ideas?
My car (05 srt-10, stock)had a tiny power steering leak from where the top hose went into the pump. It would leave a real small puddle underneath the car every day but never made the fluid level low or anything.
Well today I took the hose off and the o-ring looked ok so I just put it back on and figured Id order a new hose. After I put it back together I tried to bleed it by jacking it up and going lock to lock many times, then let it run for awhile.
It worked great for about three or four minutes then I lost power steering and fan and the car got very hot. Almost pegged the gauge. I kept repeating the bleeding procedure and nothing. So I took it back apart and put it back together and the same thing. Worked great for a few minutes then nothing. Im so frustrated, I think theres air trapped somewhere. Anyone else have this issue?
Also when I pulled the hose off, the fitting underneath the hose that goes into the pump came off. There was a bigger o-ring on that but it looked ok too. Underneath that there was a little black springy plunger thing. Not sure if disturbing that may have something to do with it?
Any ideas?